Development of a Double Action Self-Fed Cassava Peeling Machine
Table Of Contents
Thesis Abstract
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A
The federa
processing and export in 2004, since then there has been the need to improve the concept and
methods of production/processing of cassava. One of the major challenges of cassava processing
is peeling. Engineers at the Federal University of Technology, Akure, Nigeria, initiated a major
research effort to address this challenge, the effort resulted in the design of two models of a hand
fed cassava peeling machine. Feedbacks from users and the public resulted in the development of
a self-fed cassava peeling machine. Three models of the latter have been developed and reported.
In this study an appraisal of the prospects and limitations of the previous designs is presented.
The result of the appraisal was used as the basis for the design of yet an improved version of the
self fed cassava peeling machine. The machine consists of a 7Hp Honda engine, two lines of
abrasive brush, two lines of auger arranged in parallel, transmission system, frame and tuber
monitor. Further improvement was done on the existing models of the self-fed cassava-peeling
machine. Major area of improvement include, increase in the length of the peeling brush from 30
cm to 60 cm and automatic adjuster for a range of cassava tuber sizes. A double action self-fed
cassava peeling machine was developed and tested under various crop, machine and operational
conditions. The effect of brush type, speed and orientation on efficiency of the peeling process
was determined. Tubers were presented as cuttings of 20 to 25 cm long and at three different
ranges of diameters as < 8 cm, 8–10 cm and > 10 cm. Results show that auger speed of 250 to
1000 rpm resulted in peeling efficiencies of between 82 to 92% at various peripheral speeds of
the peeling brush. Adoption of this peeler is expected to (i) promote timely processing of fresh
tubers (ii) reduce labour input and (iii) increase production and hence the income of local
processors.
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Thesis Overview
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I
Agricultural En
nation through the design, production, selection, utilization and maintenance of mechanical
devices and systems in agricultural production. These efforts resulted in the development of
appropriate/user friendly devices and systems for enhanced agricultural productivity. Several
crops and products now require urgent engineering solutions. Cassava seems to be more
promising due to its potentials in Nigeria, which have been estimated at over 100 billion dollars
per annum (Agbetoye, 2003) Cassava production and processing in Nigeria and Ghana took the
central stage since 2004 through the introduction of the Presidential Initiative on Cassava
Processing and Export. Thus an enabling environment for the production, processing and export
of this commodity was created. Nweke (2004) reported that one way to make Cassava
production, processing and export a reality is to identify any cassava harvesting or peeling
machine designed for smallholders anywhere in the world and to urgently put such to on-farm
test in Africa with a view to adapt, fabricate, and diffuse it to farmers. Several efforts have been
made to develop effective cassava peeling machines in China, Brazil and in some parts of Africa
(Odigboh, 1976; 1979; Sherrif et al., 1995; Olukunle, 2005). At the International Institute of
Tropical Agriculture (IITA), Ibadan, Nigeria, the integrated cassava project initiated a search for
an effective cassava peeler in 2005. Three models (A, Band C) of a self-fed cassava-peeling
machine have also been developed (Olukunle et al., 2005). These models represent notable
improvement on the hand fed models. Major advantages include elimination of manual
intervention during the peeling process, overall reduction in drudgery and also increase in
capacity. However, peeling efficiency is generally less than 80% and losses are more than 8%.
The capacity of the machine is also less than the requirement of medium to large-scale
industrialists. In this study further improvement on models A, Band C was done in order to
enhance peeling efficiency and increase machine capacity. A double action self-fed cassava
peeling machine was designed, fabricated and tested. This model provides a dual tuber path and
specific peeling adjustment for a range of tuber sizes. The major advantage is that fewer
adjustments would be required during machine operation.
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<b>Materials and Methods. </b></p><p>
An appraisal of two mode
of hand fed and three models of self-fed cassava peeling machines
was done in order to determine the strengths and weaknesses of the previous designs. Particular
attention was placed on the global trend in the development of cassava /tuber peeling machine.
Further improvement was done on the existing models of the self-fed cassava-peeling machine.
Major area of improvement include, increase in the length of the peeling brush from 30 cm to 60
cm and automatic adjuster for a range of cassava tuber sizes. A double action self-fed cassavapeeling machine (Fig. 1) was developed and tested under various crop, machine and operational
conditions. The effect of brush type, speed and orientation on efficiency of the peeling process
was determined. Tubers were presented as cuttings of 20 to 25cm long and at three different
ranges of diameters as < 8 cm, 8-10 cm and > 10 cm. The results of the performance evaluation
were compared with manual methods.
es </p><p><b>Machine Description </b></p><p>
The double action/self
parallel, two rotating brushes 60 cm long mounted at 900 on the auger conveyors, tuber inlets and
outlets, tuber monitor, a protective hood, frame and transmission system. The machine impacts
rotary/linear motion on the tuber and thus provides the required peeling effect on the tubers as the
latter makes contact with the peeling brush. Tubers are fed into the two inlets at the same time
and the machine effects simultaneous peeling of the tubers. The resident time is governed by the
auger speed and the slippage provided by the combine action of the auger and the brush on the
tuber. It is possible to adjust the clearance in this design to obtain a tapering chamber in order to
accommodate the phenomenon of tube behaviour in the chamber. <br></p><p>
<b>Result and discussion</b> </p><p>The modifications introduced into this design are effective. Each producing desired effects on the
peeling process. The increase in brush length and hence the resident time of tubers within the
peeling chamber influenced the peeling process remarkably. The peeling brush was increased in
length from 300 mm to 600 mm. This permitted more contact with the brush as the tuber moves
through the peeling chamber. Soft - elastic material on the tuber monitor introduces higher
slippage, which is required to increase the resident time of tubers in the peeling chamber. Thus
the outer layer was completely removed in one pass of the tubers through the peeling chamber.
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The three categories into which the tubers were divided aided faster peeling process since the
tuber monitor could be adjusted only thrice, each time to handle a specific range of size of
cassava tubers. It was discovered that resident time of tubers in the chamber influenced peeling
efficiency but not independently of other parameters. Resident time of cassava tubers in the
peeling chamber was between 5 to 10 s. Fig.2 shows that auger speed of 50 to 150 rpm resulted
in peeling efficiencies of between 82 to 92 % at various peripheral speeds of the peeling brush.
This is generally higher than values obtained with Model C. While it is desirable to reduce auger
speed for higher peeling efficiency, greater challenge of adequate machine capacity arose. The
double action peeler doubles the capacity of model C by providing simultaneous peeling of tubers
in the two chambers and on the same machine. In the attempt to synchronize auger speed and
brush speed to optimize the process, it was discovered that brush speed of 1000 rpm to 1400 rpm
and auger speed of 100 to 200 rpm represent feasible ranges of speed; this is similar to findings in
Model C. However, tuber size would not significantly affect the peeling process where tubers
have been graded appropriately into correct sizes and corresponding adjustments in the inlet and
outlet clearance have been made. Maximum machine capacity was 1000 kg/hour compared with
23 kg per hour recorded during manual peeling Alade (2005) and 500 kg/hour for the hand fed
peelers. These values are feasible where average tuber weight is not less than 0.8 kg. The cost of
the prototype was estimated at 2,300 US Dollars. However, the cost of the commercial model is
estimated at 1,850 US Dollars.
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